While we were checking the springs, I also decided to get new rocker arm studs. One was missing and the rest were quite worn anyway so I got a full set. Problems started when I installed them. I removed the old and screwed in the new. At that point I noticed that at least two flanges in the head had cracks in them. The new studs were wider at the top of the threads and opened them up. Great...
Luckily I found help from the same place where the valves and seats had been machined. I removed everything from the heads and drove over to see if they could be fixed. After waiting some hours one of them had been welded. Next we tested the studs again and realized, that the new ones were a lot longer that the old. This actually proved to be a good thing because we could machine the flanges 8 mm lower. By doing that, their walls at least doubled in thickness.
I left the heads to be finalized and after a couple of days they were done. There had been three cracks in both heads and all were welded. Luckily the cracks were in the flanges and not in the combustion chamber. The threads had also been pretty bad and heli-coils had been installed in two holes. The rest had just needed some re-threading. Finally all flanges had been lowered. The results looked really good.
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Welded and machined head |
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Repaired threads |
After investigating the new studs, we realized that they were meant to be used with guide plates. The flare in the threads situated the plate correctly. As I did not use them, I needed to place a thick washers on the heads. To make sure no water would leak from the studs, I added some thread sealer and thread locker on them. Hopefully they were finally ready to be used.
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